ANALYSIS OF THE FAILURE
OF A CHILLER TUBE IN AN INDUSTRIAL BOILER
J.C.Guild:
Southern African Institute of Welding, Johannesburg, South Africa
Key Words:
Failure Investigation, Boiler, Chiller Tube, Boiler Tube, High Temperature
Failure, Steam Blanketing.
ABSTRACT
The investigation into the failure of a boiler chiller
tube is described. The failure was by way of longitudinal bursting of the tube.
It was ascribed to excessive temperatures being reached, and it is recommended
that the boiler be modified in such a way that these tubes are no longer
required.
INTRODUCTION
Two chiller tubes run horizontally along each side of
the boiler and their function is to chill slag and prevent it running into the
grate side seals. The failure had occurred as a burst in the middle of the top
tube on the west side of the boiler. At the time of failure the boiler was
idling until the next steam blow down. Although, the boiler normally operates
at 60 – 80 bar during this period, the pressure had dropped to below 60 bar and
had then been raised to about 90 bar at the time of failure. This is still 12
bar below the normal working pressure.
A previous failure had occurred in the same tube in a
similar position about a year earlier. At the time of the previous failure a
repair had been made which involved the insertion of a replacement section of
tubing approximately 1 metre in length. The failure being investigated in this
paper, occurred in this section of replacement tubing.
INVESTIGATION
The tube had failed by longitudinal bursting along
virtually the whole length of the inserted piece of tubing. This can be seen in
Figure 1.

There was considerable deformation of the tube wall along
the length of the fracture and substantial thinning of the fracture edges in
the center portion of the split. This can be seen in Figure 2.

The fracture had initiated approximately at the 2 o’clock position on
the tube circumference. This position corresponded to the grate side of a light
corrosion track, about 40mm wide, evident along the top of the tube. This is
also visible in Figure 2. The bust had followed this corrosion track except at
either end where it had slightly deviated from it. It was also evident that the
corrosion track, which had been noted at the time of the previous failure, was
considerably heavier in the original tubing on either side of the replacement
section. The circumferential tearing of the tube, which had occurred at one of
the butt welds of the inserted piece, is considered to be of a secondary nature
to the longitudinal burst. It is thought that the weld metal was probably
stronger than the tube metal and its resistance to fracture transferred the
remaining bursting energy into the plane of the heat affected zone of the weld,
resulting in the circumferential tearing. The fracture edge, itself, had a
slightly laminated or stepped appearance. This can be seen in Figure 3.

The general appearance of the inside of the tube was smooth and black
although the black oxide coating had been lost in the center portion where the
fracture was thought to have initiated from. The outside surface was generally
clean and it was noticed that there was an indentation corresponding to the
short cracks evident on the inside surface in the middle of the corrosion track
at the position of initiation. This is visible in Figure 2. When the burst
occurred it is thought that the tube hit part of the anchoring system causing
this indentation.
As far as we have been able to ascertain, these chill
tubes are listed in the manufacturer’s manual as being 76.2 mm Outside Diameter
(OD) tubes in 7 swg. i.e. 4.470 mm wall thickness. The material is indicated
elsewhere, as being carbon manganese steel to BS 3059 Grade 45S2 quality. The
original and replacement sections of tubing were both 76.2 mm OD but it was
evident that the original tubing was thicker than that used for the previous
repair. Measurements of the thickness of the replacement tube gave results of
4.3 – 4.4 mm away from the fracture suggesting that the tube was, in fact, 7
swg. Although measurements in the corrosion track of the original tube gave
wall thicknesses as low as 4.2 mm, elsewhere the thickness was in the range 5.5
– 6.3 mm. This indicates the original tubing was almost certainly a heavier
gauge. Possibly 5 swg, (5.385 mm) or even thicker.
Samples of both the original and replacement tubes
were submitted for chemical analysis. The results obtained are given in Table
1.
|
|
BS 3059 (1968) Gr 45
|
Original
Tube |
Replacement |
|
|
Element |
Specification |
Result
1 |
Result
2 |
Tube |
|
C |
0.12 –
0.18 |
0.22 |
0.23 |
0.18 |
|
Si |
0.10 –
0.35 |
0.22 |
0.22 |
0.21 |
|
Mn |
0.90 –
1.20 |
0.75 |
0.75 |
1.09 |
|
S |
0.035 max |
0.014 |
0.022 |
0.021 |
|
P |
0.040 max |
0.015 |
0.016 |
0.012 |
|
Cr |
- |
0.001 |
Not Detected |
0.05 |
|
Mo |
- |
<0.01 |
<0.01 |
<0.01 |
Table 1: Chemical composition of
tube materials.
It can be seen from the above that although the
replacement tube meets the chemical requirements of BS 3059, the original material
does not. The results do however not obviously indicate that the original
material was meant to conform to another specification.
Hardness test were carried out with the following
results:
Original tube: 140
/ 158 Hv (30 kg)
Replacement Tube: 151
/ 155 Hv (30 kg)
These figures indicate both materials to have a
tensile strength of the order of 50kg/mm2 which would meet the room
temperature test requirements of BS 3059.
Microsections were taken from various positions on the
fracture edge and also through the tube thickness at the end of the fracture.
A transverse section taken at the end of the fracture
indicated no significant abnormalities. The outside surface was oxidized to a
general depth of about 41m and there
were oxide inroads up to a depth of 85m. The
inside surface showed a thin oxide layer on the surface with some evidence of
copper deposition in the oxide. Oxide inroads were also present to a depth of
92m on the inside surface.
A longitudinal section taken in line with the burst
indicated that the steel cleanliness of the replacement section was relatively
poor with numerous fine oxide stringers and elongated sulphides. Although the
cleanliness of the steel is not considered a primary reason for failure it does
explain the laminated appearance of the fracture edge and probably, also
explains the deviation of the ends of the fracture from the corrosion track.
Sections remote from the fracture indicated both the
original and replacement tubing to have very similar microstructures of fine
grained pearlite and ferrite, typical of normalized carbon manganese steels.
Sections from the thicker part of the fracture edge indicated no abnormalities
with no significant difference in microstructure. However, sections from the thinnest
portion of the fracture edges showed substantial elongation of the grains,
decarburisation, and spheroidisation indicating that this had been the origin
of failure and that the highest temperatures had been achieved in this
position. There was no substantial evidence of creep deterioration, indicating
that the failure had been a straightforward short term, high temperature,
tensile rupture.
In view of the findings of the microstructural
investigation, calculations were performed to indicate the temperatures that
would have to be achieved to result in this type of failure. Since the original
tube had not failed and thicknesses as low as 4.2mm had been measured in the
corrosion track it was felt that 4mm was a reasonable figure to take as the
minimum figure for the thickness of the replacement section at the time of
failure. There is no evidence to suggest that the wall thickness could have
been lower than this as even on the fracture edge, readings of 4.3mm were
obtained and the depth of the corrosion track measured only 0.3mm. It was
calculated that for a 4mm thick tube at 90 bar pressure a temperature in the
range of 650 – 750°C must have been achieved prior to a tensile failure of the
type envisaged.
COMMENTS AND CONCLUSIONS
Failure occurred by a short term, high temperature,
tensile mechanism. Both the visual evidence and the calculations indicate that
this was the case and that temperatures far in excess of the design temperature
were achieved.
Although a thinner gauge of tubing was used for the
replacement section in the previous repair this is not considered to be the
cause of the failure. There is ample evidence to indicate that steam has been
generated in the top of the tube (with the consequent danger of overheating)
and this is considered the primary cause of the burst. Steam formation followed
by subsequent wetting of the oxide results in repetitive spalling and growth of
the protective magnetite layer on the inside of the tube surface thus leading
to a loss of metal thickness. The corrosion track in the top of the tube
indicates that this has, in fact, occurred. However, it is fairly evident that
at the time of the incident the amount of metal thickness lost was not
sufficient to have resulted in a failure of the type which occurred, even under
full operating conditions. It is therefore fairly certain that the failure
occurred due to an excessive rise in the tube wall temperature, just prior to
the burst, and was caused by a steam blanketing effect. As the corrosion track
appears to be present along the full length of the tube, this suggests that
poor circulation is the probable cause of the steam blanketing rather than
“hogging” of the tube. It also seems highly likely that the poor circulation is
associated with abnormal operating conditions, such as running the boiler at
reduced rates.
Since all these horizontal tubes appear to be at risk
to failure by the same mechanism, we agree that the best solution would be to
modify the boilers, such that they can be done away with. In fact, it is understood
that subsequent boilers from the same manufacturer have already had this design
change incorporated.