ANALYSIS
OF THE FAILURE OF A T JOINT BETWEEN A PROCESS PIPELINE AND A RELIEF VALVE
PIPELINE
J.C.Guild:
Southern African Institute of Welding, Johannesburg, South Africa
Key Words: Failure
Investigation, Pipeline, T joint, Compensation, Reformer effluent, Relief
valves
ABSTRACT
The investigation into the failure of a T joint where a relief valve
line was joined into a process line is described. Due to the service of the
line, a number of different degradation mechanisms were possible. These had to be
investigated before the final conclusion as to the failure mode could be
reached. Recommendations to prevent future failures are given.
INTRODUCTION
A failure had
occurred at the T joint between a 14 inch process line, containing reformer
effluent, and a 6 inch relief valve line. The failure occurred in the early
hours of the morning, when the plant was apparently running under normal
operating conditions. A considerable fire ensued and a plant shutdown, of
approximately eight days, was necessitated to carry out repairs resulting from
the failure. A previous failure had occurred in the 6 inch line, some three
months before the current failure being investigated. That failure had been
attributed to corrosion by condensed steam, resulting in severe thinning of the
pipe wall thickness. At that time the 6 inch line was replaced, and an
inspection carried out on the 14 inch line. This inspection had indicated that
no significant degradation of the 14 inch line had occurred.
INVESTIGATION
The
14 inch line carries reformer effluent (steam / hydrocarbon mixture) at
approximately 33 bar and 370°C from a waste heat boiler. Just below the top
outlet vertical bend, the horizontal 6 inch line is welded into the 14 inch
line to make a T joint. Two relief valves are situated on this line
approximately 750mm away from the T joint. The discharge lines from these
relief valves run to the main vent. Originally there was only one relief valve
in the 6 inch line, but a second was added as part of a general up-rating of
the plant.
Examination of
the failed sections of pipes indicated that fracture had initiated at the toe
of the weld between the two different sized pipes. Direction of propagation had
been at 45° into the 14 inch pipe material, and not along the heat affected
zone contour. The 6 inch line had completely pulled out of the T junction.
These features are shown in Figures 1 and 2.
The fracture
faces indicated that failure had occurred by a ductile shear mechanism.
Virtually the whole circumference had a similar 100% shear fracture face with
the shear having occurred at 45° to the axis of the 6 inch line. At the bottom
position of failure there were small areas of ‘woody’ fracture. At the top some
splitting of the 14 inch line had occurred. This is shown in Figure 3, and it
is believed to be the result of failure having occurred such that the top
section tore away last resulting in a hinge effect there. The 14 inch pipe material
was bulged outwards in the vicinity of failure, again indicating reasonable
ductility in the fracture. There was no evidence of fatigue on any of the
fracture faces.

The 14 inch line
is believed to have been in service since the plant was commissioned and the
appropriate line diagram indicated that it was constructed from ¼ inch plate.
Wall thickness measurements indicated no significant loss of thickness in the
vicinity of the failure where results of 6mm were obtained at fracture edges.
The 6 inch line was believed to have been replaced some three months earlier,
with six inch schedule 40 material and again no significant loss of wall
thickness was detected. The line diagram indicated that this T joint should
have a reinforcement pad on the 14 inch line. However, there was no evidence
that this reinforcement had ever been adopted.
Examination
of the inner surfaces of the pipes revealed a “tide” mark deposit in the bottom
of the 6 inch line with a similar deposit in a corresponding position in the 14
inch line. This can be seen in Figure 4. Chemical analysis of these deposits
indicated significant quantities of calcium and magnesium. There seems little
doubt that water has been formed by condensation in the 6 inch line on the
inlet side of the relief valves and that at some stage it has spilled or been
drawn down into the 14 inch line. It should be noted, however, that the water
was probably present in a film form rather than as a substantial slug. This is
indicated by the wide angle between the deposits on either side of the bottom
of the 6 inch pipe.
Materials of
construction for the pipes and weld metal are specified as 1 ¼ CrMo steel.
Metal analysis of samples gave the results in Table 1.
|
Sample Position |
C |
Ni |
Cr |
Mo |
V
|
|
14 Inch Parent
Metal |
0.12 |
0.06 |
1.24 |
0.49 |
0.010 |
|
6 Inch Parent
Metal |
0.10 |
0.06 |
1.15 |
0.50 |
0.006 |
|
Weld Metal |
0.07 |
0.05 |
1.26 |
0.54 |
0.010 |
Table 1: Table showing the chemical analysis of
the materials.
The
results given in table 1 are considered typical and satisfactory for these
materials and indicate no abnormalities.
Sections were
prepared for microscopic examination from several positions in the fracture
region. These revealed no significant abnormalities but served to confirm the
general assessment of the nature of the fracture that had been based on the
visual and low power microscope examination of the fracture surfaces. No
evidence was detected of hydrogen damage, creep or abnormal microstructures.
The cleanness of the 14 inch line steel was satisfactory and although that of
the 6 inch line steel was moderate / poor it is not considered to have been
significant in terms of the failure. Examination of the fracture edges showed
grain deformation confirming the ductile nature of the failure. This can be
seen in Figure 5.
Hardness testing
results are shown in Figure 6 and Table 2. No significant abnormalities were
detected.

Pos’n
|
Hardness
|
Pos’n
|
Hardness
|
|
1 |
172 |
10 |
232 |
|
2 |
181 |
11 |
241 |
|
3 |
191 |
12 |
226 |
|
4 |
206 |
13 |
219 |
|
5 |
210 |
14 |
226 |
|
6 |
214 |
15 |
255 |
|
7 |
226 |
16 |
232 |
|
8 |
247 |
17 |
219 |
|
9 |
219 |
|
|
Table 2: Hardness test results.
When the 6 inch
line had been replaced, the following “welding procedure” had apparently been
adopted:
1)
Preheat with
oxy-acetylene torch to 100 – 150°C.
2)
Weld using
KV5 electrodes.
3)
Postheat
with oxy-acetylene torch.
The use of
oxy-acetylene torch for post heating CrMo steels, or other steel for that matter,
should be avoided since little or no control can be achieved in terms of
heating rate, soaking temperature and cooling rate. In this case it was evident
that no significant harm had resulted from the post heating operation but it
should be noted that serious consequences can occur.
CONCLUSIONS AND
RECOMMENDATIONS
The 45° slanted
fracture face is typical of a ductile shear failure occurring as a result of
the resolved stress of a tensile load applied predominantly along the longitudinal
axis of the 6 inch pipeline.
The original
design specification specified the need for reinforcement of the T joint and a
study of the relevant piping codes confirm its requirement. This would seem to
indicate that this junction has been utilized close to its ultimate limit for a
considerable time. Apparently there was a front end pressure increase recorded
as initiating approximately half an hour before the failure but this increase
was only of the order of a few bar and could be considered to be within normal
limits of operation. It should be noted, however, that until approximately two
weeks before the failure, one of the relief valves was known to be passing. It
was tightened down at the time and consequently the pressure required to activate
either, or both of the valves, was substantially unknown. Possibly this was the
first pressure increase that could have activated a valve. It is known that
relief valve operation imposes a shock load to local pipe work and because of
the “under design” of the joint this may have resulted in an almost
instantaneous rupture.
It was suggested
that water could have been present in the inlet side of the relief valve and
that shock-loading conditions could have resulted when the pressure surge
forced the water through the valves. Visual evidence does not support this
theory. The tide mark deposits detected on the surface of the 6 inch line
suggests that the quantity of the water present was too small to impose
significant shock conditions.
A further
suggestion by plant personnel was that water could have been present on the
discharge side of the relief valves. This is considered feasible as water could
condense from the gas passing the valve. It has also been suggested that water
from the main vent could somehow drain back down these lines. If significant
quantities of water were present then it would seem possible that the pressure
surge could have activated a relief valve. This would then have resulted in a
sizeable shock load, both as a result of the relief valve operation and also
because of the extra forces imposed when any water was pushed through the
system.
When repairs were
made to this section of pipe work after the fire, a thicker 14 inch bend and
straight section were installed such that reinforcement was no longer required
at the T joint. Also the 6 inch line was canted at a slight angle so that water
formed by condensation on the inlet side of the relief valves would run down
into the 14 inch line and be re-converted to steam. Plans are also in hand to
provide a drain line on the outlet side of the valves.
The steps
mentioned should ensure that a further occurrence of this nature is unlikely in
this position. It would also seem wise to review other lines to ensure similar
situations do not exist elsewhere.